SRT-4 guys, help. AGP wastegate actuator.
i'll call you now.
besides it keeps me in shape,
plus, im white, 5'6, and 140lbs with a big mouth, i need to learn SOMETHING. haha
lol you can learn how to shoot *****z.keeps you in shape huh? not with that torn ACL.
TODAYS EVENTS:
first,
we removed the intake and put the boost leak tester on... found out that i had MAJOR boost leaks all over the place..
from the upper pressure pipe on cold side
upper pressure pipe on the hot side,
from my throttle positioning sensor,
among a few others spots,
-----we got it all fixed all but the TPS leak, because i have to get the OEM gasket
second,
we set out to straighten my fmic because it look like helen keller installed it with her hands tied behind her back. so after redrilling EVERYTHING we got it straight.
third,
we got my AGP solid motor mounts in. things are awsome.
fourth,
we also got my AGP wastegate actuator all adjusted to the proper boost,
fifth,
we rerouted the entire vacuum system to eliminate the PCM control of the boost to make it run more so like a normal functioning turbo system. we eliminated most of the lines, blocked off a bunch of places,
basically today we improved low end power (the motor mounts)
improved the mid range and top end with the vacuum system so the turbo doesnt spool in such low RPM's and it pulls hard up top.
great day for the neon
HUGE THANKS TO MICULANGELO (MIGUEL) AND CHRIS.
first,
we removed the intake and put the boost leak tester on... found out that i had MAJOR boost leaks all over the place..
from the upper pressure pipe on cold side
upper pressure pipe on the hot side,
from my throttle positioning sensor,
among a few others spots,
-----we got it all fixed all but the TPS leak, because i have to get the OEM gasket
second,
we set out to straighten my fmic because it look like helen keller installed it with her hands tied behind her back. so after redrilling EVERYTHING we got it straight.
third,
we got my AGP solid motor mounts in. things are awsome.
fourth,
we also got my AGP wastegate actuator all adjusted to the proper boost,
fifth,
we rerouted the entire vacuum system to eliminate the PCM control of the boost to make it run more so like a normal functioning turbo system. we eliminated most of the lines, blocked off a bunch of places,
basically today we improved low end power (the motor mounts)
improved the mid range and top end with the vacuum system so the turbo doesnt spool in such low RPM's and it pulls hard up top.
great day for the neon

HUGE THANKS TO MICULANGELO (MIGUEL) AND CHRIS.





